![]()
Miata Mailing List: September 1995, Message #96
sponsored by
From: russotto@pond.com Subject: (none) Date: Sat, 2 Sep 1995 18:00:51 -0400
I promised the list a report on the installation of my Jackson cold-air induction system, and here it is: Tools needed: 10MM and 12 MM sockets and socket wrench with extension 10MM and 12 MM combination wrenches 5/16" socket (for one hose clamp) Pliers Phillips Screwdriver Flat screwdriver Socket driver Optional tools: Torque wrench (for thermostat bolts... but whoever put them on before me obviously didn't use one...) Tentactles -- as with most jobs, having at least 3 hands is helpful, and they need to get into and around small spaces. An intelligent species of octopus would make a fine mechanic Brain - I didn't use mine much, but I should have :-) Hammer: Substitue for brain. Miata shop manual -- comes in very handy when you say "Remove WHAT?" Soldering iron, allen wrenches and multitester (see story) You start the job by removing the thermostat and dumping coolant all over the place (you didn't think it would go into the drain pan, did you?) What neither the shop manual nor the Jackson instructions told me was that there's an extra bracket in there, apparently just holding a wiring harness. I tried to reinstall it-- big mistake. I only had one of Jackson's adhesive-backed gaskets, so I used an ordinary thermostat gasket on top of the spacer. This was not a problem. Another thing the manuals don't tell you is that the old gasket will have disintegrated and you'll have to scrape it out of there piece by piece. I recommend re-installing the hoses and trying to fill the radiator NOW-- if you find the leaks at the end, you've got a LOT of work to do. Next, you remove the old intake system-- easier said than done, but not THAT hard. You'll have to disconnect one end of the upper radiator hose for this, and there's an extra bolt not mentioned in the instructions holding the intake tube to the throttle body. Also, there's an extra bolt holding the intake snorkel to the engine compartment. And, it is easier to remove the intake snorkel separately than to try to take out the air box and intake snorkel as one piece. Now you re-reroute the airbag sensor wires. Not a problem. Then you put the airbox in. Anticipating them, I removed the two bolts which would hold the "arms" of the airbox at this point. Despite what it says in the directions, don't put the airbag sensor bolt back in yet. Now you put the air meter and new hardware in. The worst part here is the accursed airbox to air meter reinforcing bar. Mine WOULD NOT FIT. This is where the hammer comes in. I eventually made it fit, though not without doing it a good bit of damage, and not without losing the bolt which holds it to the air meter. I decided that wasn't a problem, as there were a few stock bolts already removed which fit, so I used one. NOW put that airbag sensor bolt back in. Trust me, if you did it before you've removed it by now. And put the other two cowling bolts and the new washers in. Oops, I only have one cowling bolt. Right-- I used the other for the air meter. Damn and blast-- oh well, I'll leave one "arm" free until I can get another bolt. Now you have to tighten the clamps on the collapsable accordian tube, while simultaneously compressing the tube. Here's the #1 place tentacles come in handy. Now you relocate the hood rod. How do you hold the hood up while doing this? Another good place for tentacles. When it says "right side" here, in the instructions, it means DRIVER'S SIDE. I thought it meant the other side, and attached the hood bracket in the wrong place. To make matters worse, I snapped the head off that bolt (oops, guess it's a good thing they come in packages of 2!). Now I'm done-- fill up the radiator, reconnect the battery, and drive off. This is about the 4 hour mark (on a 1.5 hour job if done by someone who knows what he is doing). Unfortunately, when I fill up the radiator it leaks like a sieve out of the thermostat spacer. Turns out to be that extra bracket interfering with the seal. But now the airbox is blocking access to one of the bolts. Off comes the airbox cover, including reinforcing brackets. Off comes the air meter from the airbox. Off comes the thermostat spacer. Out comes the extra bracket. On goes the spacer, with the extra bracket left hanging. On goes the air meter. On goes the air filter and airbox cover. On go the other pieces of hardware removed. In goes some antifreeze and distilled water -- no leaks this time. On goes the radiator cap. On goes the negative battery terminal. Time to start her up! VROOM.....CHECK ENGINE. No surprise. Plug in the jumper from ground to TEN (not ground to B+, I did that before. B+ seems to be BATTERY plus. Fortunately it was only a 22-gauge jumper, and the spark burnt it right through without blowing up anything...) Code is 08, air meter shorted or open. Check connectors-- hmm, they seem fine, but reseat them anyway. Clear codes with Miata Magazine BTN fuse method. Try again. CHECK ENGINE, code 08. DAMN. Try again, shop manual yank-the-battery-and-stand-on-the-brake code clearing method. CHECK ENGINE, code 08. Step on throttle-- sounds terrible, not surprising considering it doesn't know how much air is coming in. Here's where the ohmmeter comes in. Check continuity of wiring harness extension: pin 4 is not continuous. Looks ok at the air sensor end, but the other end needs a small allen wrench to open it-- so I do. Yep, the #4 wire is broken. Yank the BTN fuse, remove the wire ties (handy trick: shove a small screwdriver into the back end and push-- pops the tie off without destroying it) and take cable inside for repairs. Repair cable, put it back together, put it back on car. Restore BTN fuse. Start engine.... CHECK ENGINE (WHAT???) Oh, it just went out! I'm in business! Reattach wire ties, adjust idle (I don't know why, but somehow it dropped), adjust freeplay on throttle (something I've been meaning to do for a while), and put away tools. That makes it to the 7-hour mark. DRIVE: Feels a little stronger from idle, though that may have more to do with removing the excess slack in the throttle cable. Doesn't feel nearly as anemic in the 2000-3500 range. Feels great above 4000--- seems to be a good bit more power. Up in that range, it sounds like hell on wheels-- it roars loudly, and vibrates badly (not suprising considering the airbox isn't quite secure...). To the fast-food joint, then to the hardware store. When I attach the last bolt, it doesn't roar as loudly, nor vibrate nearly as much. There's still some vibration, probably due to the hood rod being up against the reinforcement bracket. I'll get some foam tape later on and try and eliminate that. The one broken bolt is still broken, because I don't have a drill to remove it. It just holds the nose on, and there's lots of other bolts for that, I figure... An exhausting job, especially because of the two problems encounters. But something even a rank amateur such as myself can do.